Moistube irrigation fouling due to anaerobic filtered effluent (AF) and horizontal flow constructed wetland (HFCW) effluent
Abstract The study assessed the suitability of two effluent types, namely anaerobic filtered (AF) and horizontal flow constructed wetland (HFCW) effluent for Moistube irrigation (MTI). Secondary to this, the study determined the plugging coefficients (α) on MTI for the respective effluents. The feed...
Guardado en:
Autores principales: | , , , |
---|---|
Formato: | article |
Lenguaje: | EN |
Publicado: |
Nature Portfolio
2021
|
Materias: | |
Acceso en línea: | https://doaj.org/article/ea4e68760527466da5877928ed508e2d |
Etiquetas: |
Agregar Etiqueta
Sin Etiquetas, Sea el primero en etiquetar este registro!
|
Sumario: | Abstract The study assessed the suitability of two effluent types, namely anaerobic filtered (AF) and horizontal flow constructed wetland (HFCW) effluent for Moistube irrigation (MTI). Secondary to this, the study determined the plugging coefficients (α) on MTI for the respective effluents. The feed water was supplied from a raised tank (3.5 m), and mass-flow rates were recorded at 15 min intervals using an electronic balance. The effluent feed water concentrations and experimental room temperature (25 °C ± 1 °C) were continuously monitored and kept constant. Hermia’s models based on the $${\text{R}}^{2}$$ R 2 coefficient was used to select the best fitting fouling mechanism model and, consequently, the plugging coefficients. In addition, microbial colony analysis and scanning electron microscopy (SEM) analysis was carried out to assess the composition of the deposited sediment (DS) and adhered bacterial film (ABF) onto the MTI lateral. The study revealed that MTI pore blocking was a complex phenomenon described by complete pore-blocking model ( $${\text{R}}^{2}$$ R 2 ≥ 0.50). Discharge followed an exponential decay with early fouling observed on AF effluent because of a high concentration of total suspended solids (TSS) and dissolved organic matter (DOM). Discharge declined by 50% after 20 and 10 h of intermittent operation for AF and HFCW effluent, respectively. The α for each effluent (foulant) were $$\alpha_{AF}$$ α AF = 0.07 and $$\alpha_{ HFCW}$$ α HFCW = 0.05, respectively, for AF and HFCW. The microbial analysis revealed bacterial aggregation structures that contributed to pore blocking. SEM imaging revealed complete surface coverage by deposited sediment. It is concluded that water quality determines the operation life span of MTI, and the two effluents promote accelerated MTI pore fouling or blocking. Continuous use without flushing the MTI will promote membrane degradation and reduced discharge efficiency. Additional filtration can potentially mitigate the membrane degradation process. |
---|